stuving
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« Reply #390 on: January 14, 2020, 19:28:28 » |
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"if I'd known how late I'd be I'd have got on the TfL» train".
Isn't that the idea? Cancel the big bad GWRs▸ services, so that the oh-so wonderful Crossrail to Reading can be justified... Whose idea? Not Network Rail's - they have wanted to get the semifasts off the Main Lines since long before Crossrail was was approved to go to Reading (and even long before Crossrail was approved full stop).
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Sixty3Closure
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« Reply #391 on: January 15, 2020, 09:19:25 » |
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All good today although again pretty much standing room only by Maidenhead in carriage 4 at least.
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Sixty3Closure
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« Reply #392 on: January 21, 2020, 08:45:49 » |
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Seemed to be lots of cancellations today although the 06.54 from Twyford ran albeit late.
Not too crowded at Twyford as the Henley connection had broken down. I know it probably makes me a bad person but I gave a little smile as it meant I had a better chance of getting a seat.
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sanfrandragon
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« Reply #393 on: January 22, 2020, 07:59:03 » |
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7.07 cancelled again today. Thats a 66% failure rate this week. I dont know how to get the data, but wondering what is the cancellation (for whatever reason) rate of this service since the new timetable was introduced?
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NickB
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« Reply #394 on: January 22, 2020, 08:15:44 » |
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I was looking at this myself. For the 7.07 it is 5 cancellations since the new year and an average of 33% reliability. The adjacent trains are not much better.
I sent my official ‘this is not good enough what are you doing about it?’ to GWR▸ two weeks ago. Obviously no reply as it is still 2020. Next week I’ll be contacting my MP▸ as she ran for re-election promising improvements (not abolition) of fast commuter services.
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IndustryInsider
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« Reply #395 on: January 22, 2020, 09:19:30 » |
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Coupling issue at Oxford again this morning! Eventually left 25 minutes late as a 5-car.
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To view my GWML▸ Electrification cab video 'before and after' video comparison, as well as other videos of the new layout at Reading and 'before and after' comparisons of the Cotswold Line Redoubling scheme, see: http://www.dailymotion.com/user/IndustryInsider/
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ray951
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« Reply #396 on: January 22, 2020, 09:58:41 » |
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I was looking at this myself. For the 7.07 it is 5 cancellations since the new year and an average of 33% reliability. The adjacent trains are not much better.
I sent my official ‘this is not good enough what are you doing about it?’ to GWR▸ two weeks ago. Obviously no reply as it is still 2020. Next week I’ll be contacting my MP▸ as she ran for re-election promising improvements (not abolition) of fast commuter services.
Maybe we can have a competition to find the worst performing service since the beginning of the year I give you the 0807 Didcot to Oxford at 31% RT - 5 minutes and 6% RT (which was Jan 1st).
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BBM
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« Reply #397 on: January 22, 2020, 12:25:03 » |
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I've heard reports that the performance of the 1708 PAD» -BDW (first stop TWY▸ ) has been pretty bad so I've just checked the past 5 journeys on RTT» and found this: 15/1: arrived BDW 27L 16/1: arrived BDW 39L 17/1: terminated 30L at NBY» 20/1: terminated 33L at NBY 21/1: arrived BDW 17L
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Sixty3Closure
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« Reply #398 on: January 22, 2020, 13:04:18 » |
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The 17.08 has also run non stop to Reading once or twice which meant it was pretty empty after all the Twyford passengers got off.
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ray951
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« Reply #399 on: January 22, 2020, 14:00:10 » |
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I've heard reports that the performance of the 1708 PAD» -BDW (first stop TWY▸ ) has been pretty bad so I've just checked the past 5 journeys on RTT» and found this: 15/1: arrived BDW 27L 16/1: arrived BDW 39L 17/1: terminated 30L at NBY» 20/1: terminated 33L at NBY 21/1: arrived BDW 17L This must be a winner, since the beginning of the year the RT-5 Minutes measure has been 0% (average late 19.5 minutes) and the 1708 is 43% (average late 7.5 minutes).
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« Last Edit: January 22, 2020, 15:47:41 by ray951 »
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IndustryInsider
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« Reply #400 on: January 22, 2020, 15:43:56 » |
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Is that the one that splits at Newbury? There have been numerous problems with that at Newbury.
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To view my GWML▸ Electrification cab video 'before and after' video comparison, as well as other videos of the new layout at Reading and 'before and after' comparisons of the Cotswold Line Redoubling scheme, see: http://www.dailymotion.com/user/IndustryInsider/
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ray951
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« Reply #401 on: January 22, 2020, 16:08:38 » |
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Is that the one that splits at Newbury? There have been numerous problems with that at Newbury.
According to RTT» the service does divide at Newbury. I am surprised that GWR▸ use a class 800 on a stopping service from Newbury to Bedwyn, why not Didcot - Oxford?
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IndustryInsider
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« Reply #402 on: January 22, 2020, 16:52:27 » |
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Operational inconvenience mainly. If it was a Turbo it would be limited to 90mph, not so good in terms of the peak paths on the main line out of Paddington. If it were a 387 it would not be able to go any further than Newbury where the wires run out. Didcot to Oxford does in fact have the odd IET▸ on stopping trains, too, but usually a Turbo is the best option as it is a 90mph main line, so no speed benefit from an IET.
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To view my GWML▸ Electrification cab video 'before and after' video comparison, as well as other videos of the new layout at Reading and 'before and after' comparisons of the Cotswold Line Redoubling scheme, see: http://www.dailymotion.com/user/IndustryInsider/
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BBM
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« Reply #403 on: January 22, 2020, 17:18:17 » |
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Is that the one that splits at Newbury? There have been numerous problems with that at Newbury.
Looks like there are also problems joining it at PAD» tonight, I've just seen this on Twitter: https://twitter.com/sjm881/status/1220030275016691714Once agian the @GWRHelp 1707 padd to Bedwyn will be late as they try crashing two sets of carriages together. Platform staff watching and shaking their heads
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Sixty3Closure
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« Reply #404 on: January 22, 2020, 18:25:17 » |
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Most of the delay (34 mins late into Twyford) was caused by door problems. Announcements just said that problems closing the door meant might be a few mins delay. half an hour later we're off....
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