A surprisingly good service when compared to many lines shortly before closure. A usable commuting service from Ross to both Hereford and Gloucester.
That’s a very interesting take on the matter which led my thoughts off on all manner of tangents. I shall confine my comments to just two of them!
Firstly at the time of the Beeching cuts there was no commuting to speak of outside of the major urban areas – remember it wasn’t that much earlier that the railway were still employing young lads as “knockers up,” and there would have been precious little point in that if staff lived more than a few minutes bike ride from their place of work. No –most people lived and worked in the same area and, whilst there may have been a few commuters going into Gloucester or Hereford, it wouldn’t have been possible to run a profitable railway service o the back of it.
Secondly there is just a hint of “the railway deliberately ran the line down with the intention of closing it.” In my view this is one of those urban myths that have grown up over the years, and the final timetables before the Beeching closures do not really bear it out.
We are all aware that exponential rise of private motoring post-WW2 hit railway passenger numbers and therefore revenues hard. In general the railways continued to run as they always had – fully staffed stations, a signalbox every few miles and ditto
PW▸ gangs. It was clear that something had to give and, in view of the power of the unions in those days it would have been far easier to close a line than agree staff cuts with them.
Certainly lesser-used trains, especially late evening services, go the chop, but it should be remembered that if they had been better patronised they wouldn’t have been chopped. I do accept that withdrawing late services has a negative effect on traffic earlier in the day because potential passengers won’t make the outbound trip either, but that in itself would not prove the charge of deliberately running the line down with the intention of closing it.
The next bit is completely off topic! Having done much research on the matter over the years, I have concluded that one of the starkest examples of misplaced blame concerns the Somerset & Dorset. When you compare the final
S&D▸ timetable of 1965 with the Bradshaw 1922 reprint you find that, excluding the expresses that were diverted in 1962, the local passenger service hardly changed over those 43 years. Also remember that the expresses over the line didn’t actually serve intermediate stations, and the only people who were even mildly inconvenienced were those who wanted to go from Bath to Bournemouth and in future would have to change at Southampton.
In 1965 the S&D was being run in almost exactly the same way as it had in 1922, and in 1922 its only real competition was the horse and cart. It didn’t stand a cat in hell’s chance against the Morris Oxford or the Austin A35...
I suspect there will be some readers who disagree with all this, so let’s have a discussion